Controller communication response

Hi everyone, I'm working with a SCORBOT ER-IX. I have a LabVIEW program to communicate with robot controller (controller-B). All works fine, but sometimes, my labVIEW program enters on infinite loop
The way I work is: send a command and reads serial port until ">" char comes (controller always returns ">" at end of response). Hyperterminal works fine all times, but my programs doesn't: sometimes waits infinitely for ">" and never ends because the "Bytes at serial port" function returns "0" all time and ">" is lost.
Does someone know why this happens or how can I investigate what happens to ">"?
Thanks in advance and sorry my english.

Hi again!. I have been trying the counter solution: I have included logic in order to abort reception after 5 tries of read serial port. I'm not very satisfied with this solution, but I have noticed that even if the controller response is lost, the command is executed correctly.
I post the VIs I uses, If anybody can and wants help I will be very pleased...
Thanks!
Attachments:
FormatearComando.vi ‏10 KB
EnviarInstruccion.vi ‏45 KB
Enviar.vi ‏62 KB

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